Saturday 26th
This was our AGM day. It was good to see so many (mostly familiar) faces. After the AGM, many of us took a trip behind 2807.
There
was some discussion (in the TPO) about the loss of oil from the RH big
end. It really is a puzzle. The oil pot has a vertical pipe within it
that has a restriction through it. Oil should splash around as the loco
moves, and some will go down the pipe. At the bottom of the pipe is a
felt pad. This should restrict the flow of oil and make the pot full
last all day. So, why doesn't it? The decision was to remove the con
rod on Wednesday and have a look at the pad.
I
did suggest that replacing the cork (a plug in the top of the oil pot,
which has a cane breather through the middle) with a solid one should
create a partial vacuum and thereby restrict the oil flow. This purely
as a temporary measure until we could remove the rod.
Monday 28th
I
went over to Todders to do some chair painting - we have two or three
boot scraper orders that need progressing. 2807 was in the yard, and
the RH side con rod was positioned exactly at the angle that it has to
be when being removed. The position is fairly critical, because the
step gets in the way, and also the small end has to be backwards of the
slide bar bracket. This was either a stroke of luck, or a deliberate
act by the driver - who knows?! So, I took the decision to fit a Not To
Be Moved board on the loco!
In
this low position, the oil pot is easily accessible, so I filled it
up. Let's see how much runs out over the two day period. The oil level
can be expected to fall to that of the top of the pipe (but no motion =
no splashing, so the level should not drop below that … unless there's a
serious problem in the pot!).
I checked the Issues Log for new reported issues from Saturday. Two:
57 [JC] LH lifting link top pin loose. Pin tightened & new split pin fitted. {Thank you, JC}
72 [anon] @ cork had no core. Refitted cork. Oil usage decreased. Continue to monitor. {so much for the solid cork test - driver spotted it and replaced it with a breathable one!}
The numbering is up the creek .. it was young Jon W's fault! ;-)
Wednesday 30th
Gil,
Bruce, John G & I (aided from time to time by Loco Dept chaps)
tackled the removal of the RH con rod. The oil level had dropped to the
top of the restrictor tube (as one would have expected), so that gave
no clue about why it loses so much so quickly. It transpired that the
wheels were not 100% perfectly lined up … we had to push the loco back
by about 2". This wasn't too difficult, once the three of us were
pushing in the same direction.
The
vacuum pump has to be disconnected first (because it is linked to the
cross-head). The big end came off easily. The little end is always a
challenge, and needs an extractor. So, it took Bruce & Gil a bit
longer to get that free.
Sliding the rod off was easy. We then turned it over to be able to see the felt pad. It was in place and intact. We could see nothing wrong at all. Nevertheless, it was decided to replace the felt in both ends. I ran a wire through the constrictor, just to be sure it was not blocked. It was fine.
Sliding the rod off was easy. We then turned it over to be able to see the felt pad. It was in place and intact. We could see nothing wrong at all. Nevertheless, it was decided to replace the felt in both ends. I ran a wire through the constrictor, just to be sure it was not blocked. It was fine.
Today
was 3850's last day in service before its Heavy General Overhaul, and
John G took the opportunity to ride behind as far as Winchcombe. He was
able to report that Fred, Ray and Bill were working on the siphon
restoration. They had completed the construction of a new pair of doors
and were just making minor adjustments to its fit. They have the wood
ready for constructing the other doors, but will test this one in each
place first, just to verify that the doors are all exactly the same
size!
Bruce
cut new felt pads. These were inserted and then the con rod was fitted
back. Once again, it was the small end that caused trouble. Getting
the castellated nut lined up with the split pin hole took for ever. It
was either the nut being too slack, or too tight. Some fiddling of the
washer, nut, its castellations and the split pin finally got it all to
fit together.
We
are none the wiser as to why the oil should have run out so quickly
(i.e. after each single trip), unless … did the driver realise that the
level will fall rapidly to the level of the top of the constrictor, and
then very slowly thereafter? Maybe he thought that the pot always
needed to be full above the constrictor top? Who knows?!
During
a couple of slack periods, John G and I managed to restock the Flag
& Whistle (they having sold five boot scrapers) and do a little more
on the production line.
2807 is on Fire & Drive duty on Fridays during October. She's not rostered to be in public service now until next year.
Roger
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